India B788 at Ahmedabad on Jun 12th 2025, lost height shortly after takeoff, no thrust reported

Last Update: September 22, 2025 / 10:26:47 GMT/Zulu time

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Incident Facts

Date of incident
Jun 12, 2025

Classification
Crash

Airline
Air India

Flight number
AI-171

Aircraft Registration
VT-ANB

ICAO Type Designator
B788

Airport ICAO Code
VAAH

An Air India Boeing 787-8, registration VT-ANB performing flight AI-171 from Ahmedabad (India) to London Gatwick,EN (UK) with 230 passengers and 12 crew, was departing Ahmedabad's runway 23 at 13:38L (08:08Z), when the crew declared Mayday "No Thrust, not taking lift" (engines GENx) and the aircraft crashed into the "BJ Medical College" in Meghaninagar surbub about 0.9nm past the runway end, first impact at position N23.056 E72.612 with wreckage spread over 200 meters. Rescue services are at the scene. There have been fatalities and injuries on the ground, local police believed there was no survivor on board of the aircraft, however, later confirmed one survivor. The airline confirmed 241 people on board died in the crash, there was only one survivor. There are 19 fatalities on the ground confirmed in addition to many injuries on the ground.

The airline confirmed an incident with flight AI-171.

On Jun 19th 2025 the airline reported the aircraft had gone through major check in 2023 and was due for the next check in December 2025. The right hand engine had undergone overhaul in March 2025, the left hand engine had been inspected in April 2025. The aircraft had no issues prior to departure.

India's DGCA reported the crew called Mayday at 13:39L (08:09Z) before the crash, there was no further transmission. The aircraft carried 230 passengers (169 Indian, 53 British, 1 Canadian and 7 Portuguese Nationals) and 12 crew.

On Jun 13th 2025 the DGCA reported, that initial preliminary findings rule out a bird strike as no bird carcasses have been found. Loading of the aircraft was routine, hence a load problem is unlikely. The likelihood of a pilot error is considered minimal as is the simultaneous failure of both engines. An inspection of all Dreamliners (B788, B789) has been ordered.

On Jun 18th 2025 the DGCA stated, that the inspection of Air India's Dreamliners did not find any major safety deficiency. Aircraft and maintenance were found in compliance with existing safety standards.

Police sources have indicated, that one of the blackboxes has been recovered.

On Jun 13th 2025 India's Civil Aviation Minister reported the blackbox found at the rooftop of the doctor's hostel is the flight data recorder.

On Jun 14th 2025 Government Officials reported they have 319 body parts, both complete and incomplete. There were 33 fatalities on the ground, thus 274 in total. Recovery work is still underway. Both flight data and cockpit voice recorder as well as the aircraft's ELT were recovered.

On Jun 15th 2025 Government Officials reported the aircraft had a longer than normal takeoff run and used almost all of the 3505 meters/11499 feet long runway. 38 fatalities on the ground have been confirmed so far.

On Jun 19th 2025 India's Government stated that no decision has yet been reached where the Blackbox will be read out in reaction to media reports in India, that the black box might be send to the US for repair and analysis of the black box that had been damaged due to post crash fire so that data download in India wasn't possible.

On Jun 20th 2025 government officials stated, that India's AAIB is currently looking into another case of dual engine problems with an A321 that happened in London Gatwick in 2020, see: Incident: Titan A321 at London on Feb 26th 2020, left engine surged, engine stall indications for right engine, that was caused by fuel contamination. It appears on preliminary findings, that there was no error in the cockpit, it appears that as soon as the flight became airborne the power failure occurred leaving the aircraft unable to climb to a safe altitude.

On June 24th 2025 India's Civil Aviation Minister said: "The black box is very much in India and it it currently being investigated by India's AAIB."

On Jun 26th 2025 India's Civil Aviation Minister said, that the first black box was retrieved on Jun 13th 2025, the second on Jun 16th 2025. Both boxes were separately taken to Delhi with full security on Jun 24th 2025, the data have been successfully downloaded in the presence of AAIB and NTSB on Jun 25th 2025. The analysis of the data is underway.

On Jun 29th 2025 India's Civil Aviation Minister said: "It has never happened that both engines shut down together." Investigators are analysing the black boxes from every angle including engine issues, fuel supply problem or something else including sabotage. A preliminary report is to be expected in three months. India has accepted the proposal from ICAO for an ICAO observer into the accident investigation. The observer will not have investigative authority, but will provide technical input and ensure that global best practises are being followed. This enhances transparency and reinforces India's adherence to international standards.

On Jul 8th 2025 the AAIB indicated they have submitted their preliminary report to India's DGCA and the Ministry of Civil Aviation. The report itself has not yet been published.

On Jul 11th 2025 a reader made The Aviation Herald aware of a Service Bulletin released by General Electrics (the engine manufacturer) and the FAA: Service Bulletin FAA-2021-0273-0013 Attachment 2 issued in year 2020/2021, which recommends the replacement of the MN4 microprocessor on the ECU with respect to engine fuel and control stating: "This recommendation is to address a condition that may affect Flight Safety." The service bulletin further states: "Accumulated thermal cycles of the EEC with age causes the solder ball to fail."

On Jul 12th 2025 (India time) the AAIB released their preliminary report (currently their servers are overloaded) stating that 19 people on the ground were killed, 241 on board of the aircraft, the surviving passenger received serious injuries and continuing:

The thrust lever quadrant sustained significant thermal damage. Both thrust levers were found near the aft (idle) position. However, the EAFR data revealed that the thrust levers remained forward (takeoff thrust) until the impact. Both fuel control switch were found in the “RUN” position. (fig.13) The reverser levers were bent but were in the “stowed” position. The wiring from the TO/GA switches and autothrottle disconnect switches were visible, but heavily damaged.

Flaps were firmly located in the 5 degrees takeoff position. The APU inlet door was found open. The RAT (Ram Air Turbine) was deployed in the initial takeoff immediately after takeoff. The aircraft started to lose altitude before crossing the airport perimeter wall.

The AIB wrote:

As per the EAFR data, the aircraft crossed the take-off decision speed V1 and achieved 153 kts IAS at 08:08:33 UTC. The Vr speed (155 kts) was achieved as per the EAFR at 08:08:35 UTC. The aircraft air/ground sensors transitioned to air mode, consistent with liftoff at 08:08:39 UTC.

The aircraft achieved the maximum recorded airspeed of 180 Knots IAS at about 08:08:42 UTC and immediately thereafter, the Engine 1 and Engine 2 fuel cutoff switches transitioned from RUN to CUTOFF position one after another with a time gap of 01 sec. The Engine N1 and N2 began to decrease from their take-off values as the fuel supply to the engines was cut off.

In the cockpit voice recording, one of the pilots is heard asking the other why did he cutoff. The other pilot responded that he did not do so.

As per the EAFR data both engines N2 values passed below minimum idle speed, and the RAT hydraulic pump began supplying hydraulic power at about 08:08:47 UTC.

As per the EAFR, the Engine 1 fuel cutoff switch transitioned from CUTOFF to RUN at about 08:08:52 UTC. The APU Inlet Door began opening at about 08:08:54 UTC, consistent with the APU Auto Start logic. Thereafter at 08:08:56 UTC the Engine 2 fuel cutoff switch also transitions from CUTOFF to RUN. When fuel control switches are moved from CUTOFF to RUN while the aircraft is inflight, each engines full authority dual engine control (FADEC) automatically manages a relight and thrust recovery sequence of ignition and fuel introduction.

The EGT was observed to be rising for both engines indicating relight. Engine 1’s core deceleration stopped, reversed and started to progress to recovery. Engine 2 was able to relight but could not arrest core speed deceleration and re-introduced fuel repeatedly to increase core speed acceleration and recovery. The EAFR recording stopped at 08:09:11 UTC

At about 08:09:05 UTC, one of the pilots transmitted “MAYDAY MAYDAY MAYDAY”.

The ATCO enquired about the call sign. ATCO did not get any response but observed the aircraft crashing outside the airport boundary and activated the emergency response.

At 08:14:44 UTC, Crash Fire Tender left the airport premises for Rescue and firefighting. They were joined by Fire and Rescue services of Local Administration.

On Jul 12th 2025 (UTC) India's media report that the investigation is NOT focussing on a human action causing the fuel switches to appear in the CUTOFF position, but on a system failure. The Service Information Bulletin by the FAA issued in year 2018 recommending to upgrade the fuel switches on 737s and inspecting the fuel switch locking feature on other aircraft types including the Boeing 787 to prevent inadvertent flip of the switches, as well as the FAA/GE issued Service Bulletin FAA-2021-0273-0013 Attachment 2 relating to loss of control issue (also see above) were NOT implemented by Air India. The stated MN4 computer with faulty soldering, that might weaken and lose contact due to the thermal stress after a number of cycles, interprets data and commands fuel metering valves - with the lost contact attaching the MN4 processor to the EEC intermittent electrical contact, loss of signal processing and engine control faults can occur. The SB writes under conditions for the SB: "An LOTC (Loss Of Thrust Control) event has occurred due to an EEC MN4 microprocessor solder ball failure." According to discussions in the industry it may be possible with the number of cycles VT-ANB had already completed, the solder balls were weakened sufficiently to detach the MN4 from the EEC momentarily due to loads during the takeoff rotation leading to the loss of control of thrust and shut down of the engines.

On Jul 14th 2025 India's DGCA instructed airlines to check the fuel switches on the Boeing 787 and Boeing 737 aircraft as used by Air India Group, Indigo and Spicejet for possible disengagement of the fuel control switch locking feature according to the SAIB released by the FAA on Dec 17th 2018. The checks have to be completed by Jul 21st 2025.

On Jul 17th 2025 India's AAIB released an Appeal - in response to various media reports raising unsubstantiated claims - stating: At this stage, it is too early to reach any definitive conclusion. The investigation by the AAIB is still not complete. ... Therefore AAIB appeals to all concerned to await publication of Final Investigation Report after completion of the Investigation."

On Sep 22nd 2025 India's Supreme Court scheduled a hearing for Oct 11th 2025 to ensure the investigation is conducted in a "free, fair, impartial, independent and expeditious manner". The petition filed by "Constitution by Safety Matters Foundation" cites conflict of interest within the DGCA led investigation and alleges electrical system failure rather than pilot actions caused the crash. The petition seeks disclosure of the FDR data and CVR transcripts both with synchronised timestamps and Electronic Aircraft Fault Recording data.

India's AAIB have opened an investigation. The US NTSB and UK AAIB have dispatched teams to India to join the investigation.

Ground witnesses reported the aircraft impacted hostel buildings within a states run college for doctors, one student was able to jump out of the hotel and survived with injuries. About 50-60 students have been injured.

Local police listed 25 people who were injured on the ground and taken to hospitals. At about 14:00Z police updated there have 204 bodies been recovered and there have been 41 injured. It appears there has been no survivor on board of the aircraft. In the late evening (India time) local police confirmed a survivor on board of the aircraft who had been seated in 11A.

India's Miniter of Interior confirmed there has been one survivor. Many occupants of the aircraft are feared dead, the actual number will only be announced after DNA verification.

Relatives of the survivor in England confirmed the survivor had reported to them, but his brother was still missing.

On Jun 14th 2025 the survivor reported, that moments after becoming airborne the lights in the aircraft began to flicker and the aircraft appeared to be "stuck in the air". The lights began flickering green and white, then the aircraft slammed into a building. He saw an opening in front of him, unbelted himself and used his feet to push through the opening. Doctors treating the survivor stated, that he was disorientated and suffered multiple injuries all over his body, he is out of danger however.

BJ Medical College reported that three of their students have been killed in the crash.

The airline reported 241 people on board perished in the crash, there was only one survivor.

According to information coming from India the captain of the flight (60) had accumulated 8200 hours of flying experience, was line training captain and was about to retire. The first officer had accumulated 1100 hours of flying experience.

According to ADS-B the aircraft had entered runway 23 from the apron, which without backtracking would leave a takeoff distance available of 1900 meters/6300 feet. Four minutes later - without further position data being received, so unclear from the ADS-B whether the aircraft backtracked or not, on Jun 15th 2025 it was clarified that the aircraft had backtracked and used the full length of the runway - the aircraft took off. In the last ADS-B position the aircraft had climbed to about 625 feet MSL according to Standard Pressure (compensated for ambient pressure that would be about about 264 feet MSL or 75 feet AGL) at 174 knots over ground.

On Jun 15th/16th 2025 a tasteless and upsetting hoax surfaced on the Internet pretending to be an official preliminary report by India's AAIB carrying the date of Jun 25th 2025 (still 9 days into the future) and already "identifying" the root cause of the crash. This is fake and has nothing to do with reality, none of the information contained in this fake has any bearing to reality. India's investigation commission together with their colleagues from the NTSB, AAIB, Boeing etc. are only meeting today (Jun 16th 2025) for the first time.

Metars:
VAAH 120900Z 26006KT 6000 NSC 38/18 Q0999 NOSIG=
VAAH 120830Z 24003KT 6000 NSC 37/17 Q1000 NOSIG=
VAAH 120800Z 25007KT 6000 NSC 37/16 Q1001 NOSIG=
VAAH 120730Z 24006KT 6000 NSC 36/18 Q1001 NOSIG=
VAAH 120700Z 25006KT 6000 NSC 36/19 Q1001 NOSIG=
VAAH 120630Z 24004KT 6000 NSC 34/19 Q1002 NOSIG=
VAAH 120600Z 22002KT 6000 NSC 34/20 Q1002 NOSIG=
VAAH 120530Z 25006KT 6000 NSC 33/20 Q1002 NOSIG=
VAAH 120500Z 29005KT 5000 FU NSC 32/21 Q1002 NOSIG=
VAAH 120430Z 30005KT 5000 FU NSC 31/21 Q1003 NOSIG=
VAAH 120400Z 28006KT 5000 FU NSC 31/21 Q1003 NOSIG=
Incident Facts

Date of incident
Jun 12, 2025

Classification
Crash

Airline
Air India

Flight number
AI-171

Aircraft Registration
VT-ANB

ICAO Type Designator
B788

Airport ICAO Code
VAAH

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This article is published under license from Avherald.com. © of text by Avherald.com.
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